87' VG30I
I recently tore apart my throttle body to have the injectors rebuilt. Despite the other problem it created I have noticed much better throttle response and more overall power. However, it seems as thought I put something back together wrong.
If I'm not mistaken the Mass Air Flow sensor is the black plastic case with two diodes sticking out that is held onto the upper throttle body by three screws. I removed this and all other components before soaking the upper throttle body in parts cleaner for 7 days.
After I cleaned everything up and added new gaskets I noticed that my motor now bucks like a 383 stroker engine at 300 rpm. It also isn't quite what it used to be as far as power goes, much better than with better injectors, but not like it should be.
Upon checking the ECU it gave a code 12, Mass Air Flow sensor. I know I didn't break it when I took it out, I know they are expensive so I was careful with it. All I can think of is that maybe the wire harness is corroded enough to where its not fully functioning.
Any ideas? Has anyone else ever had this problem?
I recently tore apart my throttle body to have the injectors rebuilt. Despite the other problem it created I have noticed much better throttle response and more overall power. However, it seems as thought I put something back together wrong.
If I'm not mistaken the Mass Air Flow sensor is the black plastic case with two diodes sticking out that is held onto the upper throttle body by three screws. I removed this and all other components before soaking the upper throttle body in parts cleaner for 7 days.
After I cleaned everything up and added new gaskets I noticed that my motor now bucks like a 383 stroker engine at 300 rpm. It also isn't quite what it used to be as far as power goes, much better than with better injectors, but not like it should be.
Upon checking the ECU it gave a code 12, Mass Air Flow sensor. I know I didn't break it when I took it out, I know they are expensive so I was careful with it. All I can think of is that maybe the wire harness is corroded enough to where its not fully functioning.
Any ideas? Has anyone else ever had this problem?